When Power Jets personnel went to USA in October 1941 they also took the plans for the W2 with them.
Via the Ministry, Hooker would read GE of America's reports on progress as indeed they would have read Hooker's reports on progress here.
Early 1944 saw an invitation arrive from Col. Don Klein of the USAAF for a party of Brtish engineers to vist the USA and see first hand what progress had been made in America. The GTCC set up the team, Hayne Constant of RAE headed the party which included David Smith from Metrovick, Leslie Cheshire of PJ, 'Pat' Liindsey of Armstrong Siddeley, Moul, Brodie and Clarkson from DH and Hooker from RR.
Leaving Liverpool in April 1944 the team travelled aboard an almost empty US Coastguard troop carrying ship Wakefield that zig-zagged at 18 kts across the Atlantic to Boston. The first visit was to GE at Lynn near Boston, home of the I series of Whittle centrifugals. Hooker was taken aback when he saw the I-40 straight through turbojet. Unlike Barnoldswick not only had thay straightened out the gas flow they had gone for a greater thrust level. Designed at 4,000 lbt, at the time of the visit it was delivering 3,750 lbt. 103 inches long with a diameter of 48 in it had a double sided impeller of 30 in diameter and 14 combustion chambers delivering hot gases to a turbine of 25.9 in dia and a blade height of 3.95 in. The rpm was 11,500 and AMF was 76 lb/sec; sfc was 1.19. GE had begun designing the I-40, the successor to the-16, in March 1943 and had run its first test on January 8, 1944.
Hooker resolved to do something about this when he returned to Barnoldswick.
The Halford H-1 or de Havilland Goblin was designed to achieve around 3,000 lbt so Hooker resolved to leapfrog that too.Hooker was back in the office at the end of April and discussed his thoughts with Group Captain George Watt of RNZAF who had taken over the GTCC chair fron Roxbee Cox. "George I want to build a 5,000lbt engine," said Hooker, "we must get cracking or the Americans will beat us to it."
"Are you sure it should be as much as 5,000lb?" came the reply.
"Of course not. Le tus say a figure of 4,200 lb and we will design for 5,000."
"OK, I will issue a specification for 4,200 lb. and you can go ahead now. If you get 5,000lb so much the better."
May !st saw Hooker, Lombard, Pearson and Morley set out to design and produce the engine. This was the first time the team had a clean sheet of paper. They felt they had much experience and so should be able to come up with a better turbojet. Lombard had already looked at a project for a MAP fighter spec. that Hawker had responded to with a version of the Fury, the P.1031 with an RB40 jet in the nose. The RB40 was a √2.6 scale up of the Derwent. The airflow was set at 100 lb/sec and the dia of the engine came out at 55 in dia 100 in long to the end of exhaust cone, with an impeller diameter of 32 in.
Now with Hooker's clean sheet approach and a great deal of Derwent experience they were able to start at 80 lb/sec flow and with the best impeller design they could achieve came up with a dia of 28.8 in. Using Whittle's W2/500 diffuser design was also the most efficient design to date. The turbine disc and its bearing had never been properly cooled so a small centifugal comprssor was added specifically to address this issue. The straight-through combustion chambers were designed by Stanley Clarke at Lucas. He managed to reduce the pressure drop and improve efficiency over what he had achieved on the Derwent.
Bt the summer drawings were being released to the shop and the overall diameter was coming out at 49.5, a full 5.5 in behind the target value set by the RB40. The engine weighed in at 1,600 lb way below the 2,200 target weight. Manufacture and assembly proceeded at a fast pace, with the flying bomb attacks on London giving renewed impetus. The engine was ready to test on 27 October 1944. Last minute adjustments took all day and it was 10 pm before the team were ready to press the button and start the engine.
The light up procedure for a new engine is:
Using a large electric motor the engine rotates pressurising the fuel supply. At a certain pressure the fuel shut-off cock is opened so that fuel sprays into the combustion chamber when two igniter plugs, essentially big spark plugs are fired and the combustion process starts. The positioning of the igniters is a key factor and is a trial and error procedure. The positioning on the RB41 prototype was wrong and the first two attempts were a failure. The team's ignition experts, Dizzy Drew and Ballantyne, knew a quick fix. They removed one of the ignitors and an oxy acetylene welding torch was stuffed down the hole. The engine started with a bang and was soon running smoothly. The pair had invented the torch ignitor! By midnight the engine had been checked out and slowly opened up to deliver 4,000lbt. Hooker stopped the test and all repaired to the canteen to have a celebratory sausages and mash. Although Denning Pearson had pleaded to have the staic IGVs on the first runs Hooker had overruled him as he did not want a risk of damage from pieces falling off. This meant the 4,000lbt was achieved at maximum allowable temperature and so Hooker remarked there was little hope of achieving 5,000lbt without more development and then went home to bed. The next day when he arrived at work he could hear the Nene running. On arrival at the test bed he saw it was running at the same temperature as last night, but delivering 5,000lbt! Pearson had his IGVs fitted overnight and the improved efficiency enabled the target to be reached.